Monday, May 2, 2016

Trail & Error



Last week while working on our robot, we realized that our original design to pick up the racket ball wasnt working as well as we thought. The motor wasnt able to spin the gears because the design was slightly crooked. We decided that fixing it wouldn't be successful so we abandoned the idea entirely and started anew. We bent a single piece of flat metal and connected the motor to a rubbery gear. The design works very well now. Success!

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